This incident occurred during leak testing in connection with maintenance work with a choke valve on one of the wells.
Derived from a shut-in volume above the downhole safety valve in the well, the gas leak had a high initial rate of 1.2 kilograms per second and lasted for an hour. A serious condition thereby arose on the installation.
The PSA’s investigation team will be travelling to Gullfaks B on the afternoon of Monday 6 December.
One aim of its work is to ascertain the course of events and identify the direct and underlying causes. This will result in a report to be published on the PSA website.
Øyvind Midttun, Press contact
Email: firstname.lastname@example.org | +47 51 87 34 77